The last few weeks have been very busy personally, so to make progress on the Nova I've been doing a bunch of very short (<30min) trips to the garage. One day I filled the diff:
Another day, I put the rear brake lines back on the axle and connected everything.
Some other day I loaded the brake pads (Hawk HPS) and bolted down the calipers
With the rear lines finally all connected, I could turn my attention rearranging the mess shown below. These are the factory disc/drum hard lines around the master cylinder and distribution block for my '70 Nova. I decided I want to keep the original distribution block because it has an integral brake warning switch that triggers an idiot light if there's a pressure imbalance between the front and rear. Once I had a leaky master that went unnoticed until the brake light started going off near the bottom of pedal travel, so I decided I want it to function. If you don't care for that feature, there are a few great aftermarket combo valves that incorporate the distribution block with a proportioning valve and keep everything tidy. Some have a brake light switch, but that is a different function from the switch this block has.
I forgot to snap a photo, but my system originally had a fixed proportioning valve on the side of the subframe, which I needed to replace with something adjustable for the new disc/disc combo. For now, I decided to keep the original style master cylinder even though it was made for a disc/drum application. The main difference between a disc/drum and a disc/disc master is the size of the rear reservoir and the potential inclusion of a residual pressure valve in the rear port. A disc/disc master has a larger rear reservoir to accommodate pad wear which normally isn't a problem for a drum rear system that has a mechanical adjuster to take up wear. This means I will have to keep an eye on the rear reservoir level as the pads wear, but most likely I will replace the master before there's a dramatic change.
I expected to find a residual pressure valve in my master's rear port, but after pulling the lines I found a drill bit could insert right through, indicating the spring/valve mechanism was not installed. This is a reman master and I've heard they often left the valves out.
The next task was finding a suitable location for the new adjustable proportioning valve. It wouldn't quite fit under the master due to little space between the master and distribution block. My favorite spot was directly next to the master cylinder, but I could not figure out how I'd mount it. So I finally decided to secure it to the inner fender with a pair of rivnuts.
Next I carefully replicated most of the bends of the factory hard line that ran from the distribution block down to the original proportioning valve that was on the frame. Getting that line in and out past the steering box and between the floorpan of the car was a total PITA, but having it in position gave me a point of reference to make the last few bends to the valve.
The factory uses spiral/coil loops and/or S-bends to provide strain relief near connections like these. This makes the tubing more flexible so it can be installed easily and adjusted for misalignment. To make my own coil, I grabbed a used differential crush sleeve and simply wrapped the tubing around it by hand.
Here is what the line looks like installed. It runs from the outlet of the proportioning valve down to a coupling by the subframe which replaced the original proportioning valve. From that coupling it connects to the original line and runs to the rear, where it connects to the softline that takes it down to the differential.
The stainless steel spring stuff around the brakelines is for abrasion resistance and general protection. I put it on the tubing and cut it to length before adding the last fitting and flare. It can be a challenge to get the tube into the flaring tool while the spring is trying to push the fitting off. To keep the fitting out of the die, insert an open end wrench between the die and the fitting.
My 7yr old son made the last line at the front. I helped him measure and mark and let him make all the bends and flares himself. It could definitely be more tucked, but I'm happy with how it turned out.
Once that was all together, I used a one-man bleeder (tube with check valve and small reservoir) and worked to clear the system. I started with the rears and it took damn near 100 pumps of the pedal before fluid starting coming out. Dry systems are always a bear! Some day I'll get a better tool for bleeding. The little bit of fluid that was still in the used calipers came out a little cloudy but not too bad. Eventually everything was flushed clear with new dot 5 silicon fluid. I swear by the stuff because it doesn't eat paint and it works fine for my use.
All this occurred over a few weeks and a series of short trips to the garage. I don't think any two of the brake lines were made same day. Family time is my priority, so progress on the car is slow.